The
kit arrived in a substantial box (well it must have been in times past but
this box was somewhat battered) containing various sheets of etch, one of
them 0.9mm thick nickel silver, various castings, nuts, bolts, wire and top
hat bearings. There are many pages of instructions, diagrams, parts list,
historical notes and etch maps. Clearly this kit has a long history and has
passed through a number of trader's hands. It was originally drawn by one
George Norton, whom I am told, was one of the pioneers of etched kits. It
was probably state of the art in its day but of course, looks a little crude
beside the best of current efforts. There are a few tab and slots but much
of it requires edge soldering.Also in the box were a set of suitable Slater's wheels, numerous extra third party castings, a set of Meteor Models horn guides and a pack of Slater's etched steel connecting rods to suite the wheelbase. My client had picked up the whole lot as bargain at a show. All it needed was a motor/gearbox, which was duly ordered from ABC.
The
original intention had been to use the Slater's etched rods in lieu of the
rather heavy set in the kit. Those in the kit are designed to pivot on the
centre axle with a dummy pivot in front of the centre driver. The Slater's
set is designed to pivot in the correct place but proved to be very poorly
etched and were returned. Slater's rapidly replaced them without question,
though they must have been originally bought some years ago. Unfortunately
that set proved also to be totally unusable as this picture illustrates, so
I modified the original set to pivot correctly instead.
Back to topAfter laminating the original rods and cleaning them up I joined them using cocktail sticks and drilled right through the pivot boss in both laminates. Then the rear part containing the crankpin hole was cut off and soldered to the back of top overlay. Further careful cleaning and polishing before riveting each half together resulted in a set of rods that were acceptable. The only part I used from the Slater's etch were the rivets! This picture, shews all the parts required for the chassis cleaned up and ready for assembly, including the finished rods.
The
frames were drilled out between the forward pair of horn guides to take some
2mm rod for the compensation beam. The wheels had their backs carefully
rubbed down on a sheet of 240 grit wet & dry fixed to a sheet of plate glass
until the centre brass boss and rim were level. This is important to ensure
that the wheels run as true as possible and is necessary because of the
limits of manufacturing tolerances in the way they are made.
Both
sets of rods were then set up in the Master Chassis jig to prove they were
accurate and to set the dummy axles at the correct spacing. Once this is
done the dummy axles can be locked down and the frames offered up. It is a
simple matter then to assemble the frames and bearings square.
This picture shews the frames assembled with the bearings and horn guides
all fitted.The compensation beam is a piece of 1x6mm brass stock suitably bent to shape after annealing, it needs to be relatively soft so that adjustments can be made to ride height after fitting. Back to top
The beam is simply soldered to a piece
of brass tube that pivots around some 2mm brass rod soldered between the
frames. I chemically blackened the ends of the tube before fitting it and
the rod to prevent them locking up solid. Simple and effective.
The next job was to set up the wheels and rods and test the rolling
chassis. It worked first time and runs sweetly. The 12BA nuts holding the
rods in place will be replaced by cast nickel silver crank pin nuts from
CPL. Yes, I know they are Great Western but they will look immeasurably
better than those awful nuts. The ABC motor/gearbox duly arrived so
running-in could begin. I set up the shims to prevent excessive side play
in the wheels and continued to add further parts.
Setting up the pony truck is relatively simple but the guard irons are, I
think, much too thin. Unfortunately the axle for the pony truck had a
defective shoulder so one wheel was seriously out of true. I sent it back
to Slater's expecting it to be replaced however, they declined on the
grounds that the set must be at least ten years old. I had never considered
there was a statute of limitations on poor quality control. Granted I did
not send the packing, it had been dumped some days previously but, it was I
think obvious that the set had never been used. Big black mark to Slater's.
Back to top
Brakes. The brake blocks should really have a good deal more thickness than
the two layers provided both to look better and to fit the brackets they
hang from properly.The instructions mention brakes with inside rods but give no guidance about them at all. My client's engine (No: 1618) had inside rods plus, I wanted the brakes to be removable for ease of maintenance and painting.
Most of the fixing holes are far to big for the 0.9mm wire intended to fit them so I opened out the holes in the frame to take 1.5mm OD brass tube. 7mm lengths were cut and one end de-burred inside and out and then soldered into the frames, leaving about a 1mm standing proud. The brake shoes and hanger brackets were fixed to short lengths of 1.1mm rod to fit in the tube. These two pictures illustrate the parts well.


Next the brake rigging was set up using 1.3mm rod as shewn here ready for
soldering. Ensure that the brake rods are the right way round with the long
ones in the centre.The ends are then supposed to be soldered to the bracket visible in the next picture under the plate that holds the pony truck. It is designed for outside rods so needed cutting down and soldering in two halves as shewn here. Back to top
The rear rods can be cut in unequal halves with one segment soldered to the spring and the other securely soldered to the cross bar in front so that it is horizontal. Once completed, it is invisible from normal viewing angles.
So here is the chassis with the brakes completed awaiting a replacement
wheel set for the pony truck and the motor/gearbox. As usual, I made it up
as I went along. One of these days I shall get caught out.THE BODY
The footplate needs careful cleaning up and I found that the section at the
rear that fits between frames required considerable filing down to get it to
fit in. The instructions suggest edge soldering the valances and buffer
planks into position but I decided to beef up the joints. It was then much
easier to get them straight and vertical and also helped stiffen up the
footplate too.A line was scribed on the underside of the footplate; the sides at 1.8mm - 1.3 clearance plus 0.5mm for the thickness of the valance - and 2.6mm at the ends. Inside this line I soldered four lengths of 1x2mm flat brass bar. Back to top
The valances come in two parts and it is important carefully to measure and
cut off some the half etched length from both parts so that the parts fit
properly. The buffer planks were soldered in place first and the valances
fitted between them. Once cleaned up and a couple of 8BA nuts were soldered
over the body fixing holes it was time to try it for fit on the chassis.
This close-up shews how the supporting structure was put in place. The
front of the frames needed notching to fit over the extra metal. Now that I
had a square footplate that fitted properly on a square chassis, work began
on the body proper.
However, before starting that I took time out to fit the buffers. These are
nice brass turnings with integral sprung, steel heads. The instructions say
to mount them with part 24 and shews this part as fitting between the buffer
body and the buffer beam. In fact part 24 is a nice circular etching with
four bolt heads and is clearly supposed to fit over the base of the buffer.
It has a hole that is too small to fit over the buffer body shank. Opening
the hole out to fit over the buffer housing is a real trial of patience and
careful handling since the metal is about 0.25mm thick! Once the hole is
made large enough the burr was carefully filed off before the etch was
soldered to the buffer base and the edges filed down. Each buffer was glued
on the beam using Loctite 480 carefully lining up the bolt heads to be the
same. Back
to top
I fitted the beading to the cab while it was in the flat, much easier and it
can be soldered from the inside. I also fitted the handrail stanchion to
the tank front. It was necessary to file the tank front so that the
stanchion was rebated into it to be level with the top edge. The tanks can
be reduced in size to produce different versions and there are half etched
lines to work to but I am building the large tank version. The spectacle
rings were also fitted at this stage. Here then are most of the parts
required to build the body ready for construction to begin.
The tank tops are supposed to be edge soldered 0.9mm below the top edge of
the tank side. However I decided to solder it the other way round with one
leg of "L" soldered to the side for strength and to fill in later with a
full side piece instead. To get the end to fit neatly I filed the tank top
to fit the base of the handrail stanchion. I could have soldered the
stanchion to the tank top instead but so long as the end result is neat it
does not matter much. The tank fronts were then soldered in place as shewn
here.
This made fixing the tank and cab side to the footplate easier. I used the
cab front - but not soldered in yet - to help locate this part as well as
the front of the coal bunker. It was tack soldered first, checked for
square and then seamed up. You can see also that I have fitted the front
splashers. They are not difficult, if one is used to edge soldering.
Back to topThe other side tank and cab was next fixed followed by the cab front. This is too short to be soldered to the footplate using the tabs and slots provided. I assume to cater for the small tank version. It requires some care to get fitted square. The bunker back was fitted last after having checked that all was square.

The handrails for the cab are a good fit but the holes in the footplate for
those at the front of the tanks are out of alignment so I filled them with
solder and simply soldered the base of the wire to footplate. I will see if
they prove to be strong enough, if not it will require measuring up and new
holes drilling in the footplate.
The brass tube supplied for the boiler needs a section removing for the
motor space. I used the mini-drill with a heavy duty cutting disk, the job
wore-out 2 disks! Once completed the cut edges were cleaned up and rounded
off to avoid damaging wires.
The holes have now been drilled for the major fittings and handrail knobs.
The dome, chimney and safety valve have been cleaned up for later mounting.
Still to do are various holes for pipes and valves. In fact I replaced the
chimney with another that had a hole all the way through.
Back to topMarking up was a pain, I ought to have done it with the tube set up in the lathe, before fitting the smoke box and cutting the motor space.
The handrail knobs were then soldered in using some straight wire to line
them up. Some care is needed because one needs enough heat to combat the
huge sink of the boiler but not melt the knobs. Plenty of flux also helped
too.
All holes are drilled now for the various fittings on the side and top of
the boiler. The brass ring that goes behind the smokebox was particularly
difficult due to the huge heat sink the boiler makes. After three attempts
at soldering I glued it with Loctite 480. Lastly, a millimetre or so needed
to be cut off the cab end to allow the backhead to fit.I am told by John at Fourtrack that this kit now comes with an etched boiler so it ought to be far easier but the sequence may be different. Back to top


The roof is made up from two parts, the open square being larger than the
roof proper. They are almost square so it is important to get them aligned
properly. The other two pieces shewn were fashioned out of some thick
nickel silver sheet and will serve to hold the roof in place.The centre view of the underside of the roof shews the holding lugs soldered in - they just fitted nicely inside the square - and the wire used to hold the vent open. The other picture shews the top with the vent fitted and the whistles fitted too. Bending this part might have been a problem due to the etched in rainwater strips so rollers were avoided. I annealed the part and bent it in my fingers, soldered in the square part, checked the curve and soldered in the lugs. It is a snug fit on the cab.
The body is now close to being completed, only the sand pipes, sanding rods
and lamp irons remain before fitting the boiler.
Here is the completed engine waiting for a trip to the paint shop. When my
client has painted it I will get some more pictures of it. It weighs in at
1lb 9ozs but there is room for lots of ballast if required in the tanks and
the front of the boiler. The upper, rear, lamp iron is difficult being made
up from three parts that need soldering in a slot in the bunker back. In
the end I soldered part of the bracket to the bunker back and used Loctite
480 to fit the rest.
Back to topAn attractive little engine, it proved to be an interesting build but I would not recommend it for beginner. The next job for this client will be an N8 using an original George Norton kit we found recently at the Langley show.
Here it is again running on its home layout "Staindrop" in need of a crew
and lamps. It is owned by Chris Robertson, Chairman of the Epsom & Ewell
MRC.Back to top